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> redtop 3sge woe's
post Sep 24, 2013 - 10:24 PM
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rdyzz

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the long

so my engine has been running like its on two maps or somthing. it started doing this after the last track event in july, i've been trying different things on it since then. its a redtop 3sge im wondering if anyone has ever had an engine of theirs do this. i feel like im chasing a ghost since every time i think i make break through it seems to come back. first diagnosis was on a dyno, testing for air fuel ratio, in 4th gear at wot around 2,000-4,000rpm the air fuel was in the 17's and then got to about 11.9 at redline. lowering the spark plug gap to 1.0mm seemed to have made a difference there. i then installed a fuel pump after and it seemed to drive well for the most part, i then replaced the fuel filter a week after the new walbro 190 pump. did an on car injector clean with an on car cleaner kit. the car still occasionally hesitates in 2nd gear or 3rd gear at 1/4 throttle if i was to give it quicker throttle inputs. at the moment i got more parts comming, COPS and a new vvti cam pulley. i just dont understand why an engine would do this, you can feel the difference in throttle response.


the short

symptoms. intermittent hesitation 1/4 throttle, or quick throttle inputs. drives like it has power, then drives like it lacks engine torque at times. certain times WOT in 1st from a roll will be super powerful you have to hold onto the steering wheel to keep car straight, other times same 1st gear roll will feel less powerful by quite a bit.

what i have done.
- fuel pump, walbro 190
- new fuel filter
- adjustable fuel pressure regulator set at 43psi
- new tps sensor
- tested with new water temp sensor
- tested 1mzfe maf, swapped maf, 1mzfe car still ran fine
- checked most connectors and repaired any cracks in insulation
- new 2 ga ground cable
- cleaned fuel injector with on car injector cleaning kit
- seafoam oil, ran in fuel tank also
- o2 sensor is 1 year old
- new spark plugs
- inspected vvti solenoid, its clean and functions
- checked for vacuum leaks

what i have not tried yet.
- new COP
- new vvti pulley
- knock sensor
- new ecu

i dont know if the cam angle or crank angle sensor has anything to do with this. it doesnt have any symptoms related to these two.

thanks for any insight.
post Sep 24, 2013 - 10:36 PM
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Batman722



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- fuel pump, walbro 190
- adjustable fuel pressure regulator set at 43psi
- new tps sensor

First, why did you do these things ^^ ?

Next, do you have the stock air box ?
What do you have for an exhaust ?
Any CEL ?
Have you done a compression test ?


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post Sep 24, 2013 - 11:17 PM
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njccmd2002



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^^^ listen...... listen


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post Sep 24, 2013 - 11:33 PM
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perkyshadow



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When the BEAMS first went it, it has some crazy hesitation at times. The issue was a slightly frayed O2 sensor wire. Last month, it was idling high, and didn't act quite right. It was a stuck Idle Air Control Valve. I had several guys suggest the IACV, and they noted that it can cause several different issues!
post Sep 25, 2013 - 7:53 AM
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rdyzz

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compression tested 180, 175, 175, 170. it was just me cranking on my odyssey 680 and no one to look at the gauge.

the fuel stuff was changed in due to the dyno tuner being a friend and ase certified tech suggesting the old 220,000 mile original fuel pump did not have the initial burst of pressure and thus cuausing the lean initial throttle. the car was like this after a track day, 5 20min heats.

so i chased the fuel system more since at first the walbro did improve the initial throttle response and torque, however somtimes when it ran strong with partial throttle the transition to full throttle almost seemed it leaned the car out or over flooded the car. and other times when its less responsive the transition to wot will accelerate like crazy.

when it drives strong it drives like it should making you feel "this is how it should be", but when its bad you can tell.

also yes i know my iac is acting up, i can hear it sounding like a drill when you barely touch the trigger. just didint think it had this much affect on the car since it just bypass air for idle. all the master techs at the toyota i work at say the IAC has nothing to do with response or power thats why i never bothered to look here. somtimes engine idles at 500rpm.

exhaust is 2 1/4 with an mangnaflow muffler.

intake is factory maf section cut for a cone filter, i've ran the sard and 1mzfe before this with no difference. i also have no cel.


This post has been edited by rdyzz: Sep 25, 2013 - 12:30 PM
post Sep 25, 2013 - 3:59 PM
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BonzaiCelica



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dude all N/A 6gc have same fuel pump! i learned the hard way don't worry.

aahh fail i thought we were talking about 6gc

This post has been edited by BonzaiCelica: Sep 25, 2013 - 7:42 PM


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post Sep 25, 2013 - 5:41 PM
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richee3



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He has a Corolla. It was necessary to replace the fuel pump.


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"Employ your time in improving yourself by other men's writings, so that you shall gain easily what others labored hard for." -Socrates. Even Socrates told us to use the search button!

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post Sep 25, 2013 - 5:51 PM
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rdyzz

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so i sprayed some carb cleaner into the iac port and it seemed to have made a difference. without the air filter and the tb exposed i can clearly hear the drill like noise.
i took it off to clean it further. it seems like the motor might of been from a different car since whoever had this engine before me did this. the motor seemed to have been modified to fit.
post Sep 25, 2013 - 6:54 PM
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richee3



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You can use an ISCV from a 2000-05 Toyota Echo. They can be picked up from Rock Auto for like $150 or from Toyota for like $250.


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"Employ your time in improving yourself by other men's writings, so that you shall gain easily what others labored hard for." -Socrates. Even Socrates told us to use the search button!

2006 Aston Martin V8 Vantage.
1998 Celica GT-
BEAMS Swapped.
2022 4Runner TRD Off Road Prenium.
2021 GMC Sierra AT4.
post Sep 25, 2013 - 8:53 PM
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rdyzz

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thanks richee3, well see if this does anything. i took off the iac and cleaned it pretty well. the pn on the motor is 22270-7437 and the last number is shaved, the beams ends with a 0. looks like whoever owned it before me did somthing to this motor. the area the screws goes on has been cut, so they can turn the motor more counter clockwise, if that makes any sense. the screws are holding it by washers instead now. when i took the thing apart the gasket seemed longer than normal, i had to run to the other side of town to another toyota dealership to get new gaskets.

since the cleaning it doesnt seem to make the drill like sqeak anymore. hopefully this does it.

btw richee do you just use the motor off the echo? i notice the 1zzfe ones look really similar, except it has 2 coolant hose and maybe the screw placement might be different.
post Sep 25, 2013 - 9:19 PM
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richee3



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I haven't had a chance (translated: funds) to replace mine yet. I know the stock ISCV can be turned and adjusted like most TPS's. My ISCV is just about done for. My idle isn't far off but isn't great right now. Cleaning it helped slightly but it's beyond cleaning this time.

Has the BEAMS Owners Group been down for you too? I usually check it every morning but haven't been able to pull it up lately. I've just given up the last few days.


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"Employ your time in improving yourself by other men's writings, so that you shall gain easily what others labored hard for." -Socrates. Even Socrates told us to use the search button!

2006 Aston Martin V8 Vantage.
1998 Celica GT-
BEAMS Swapped.
2022 4Runner TRD Off Road Prenium.
2021 GMC Sierra AT4.
post Sep 25, 2013 - 9:46 PM
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rdyzz

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beams owners sites been down for me as well, the car drove well for two days and sunday it started acting up again. shifting gear at times cause a stumble when i add throttle. this is very annoying i was gonna buy a spare motor cause i thought this engine was dying, but when it drives right its so enjoyable and it convinces me to keep trying to figure out whats wrong with it. spending money on the afpr stuff and cops and vvti pulley has all added up close to what a spare would cost lol.

theres a track event next week i wanted to drive in, thats why i was pushing so hard to fix this, but now it looks like i may have to wait for the winter to pass and fix this during then if its not the idle control.
post Sep 25, 2013 - 11:41 PM
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Outsider



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new BEAMS forum link

This link still works for me


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post Sep 26, 2013 - 9:18 AM
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aspen

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The BEAMS Owners Group URL Changed. The Google indexes haven't caught up yet.
If you start from mr2.com, you can get there.


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post Sep 26, 2013 - 9:57 AM
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richee3



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Nice, that explains it. I keep a tab open in my phone for 6gc, my350z, and the BEAMS Owners Group. Never really bother to navigate the rest of mr2.com.


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"Employ your time in improving yourself by other men's writings, so that you shall gain easily what others labored hard for." -Socrates. Even Socrates told us to use the search button!

2006 Aston Martin V8 Vantage.
1998 Celica GT-
BEAMS Swapped.
2022 4Runner TRD Off Road Prenium.
2021 GMC Sierra AT4.
post Sep 26, 2013 - 6:02 PM
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rdyzz

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thanks guys for adding the link i thought the site was down.

so after cleaning it yesterday, the morning seemed like it drove strong. then at lunch time i went for a drive and it did the same thing again. so after work i went and got some new fuel return line and reinstalled the oem fpr, since the aeromotive one had 6 AN fittings and some earls 90 degree swivel fittings to adapt to it, but was leaking no matter how i clean the mating surface or tighten it up. actually i had it snug and had the car idling and i would tighten little by little to see if there was less leaking, but it got to the point i thought the fittings were going to strip and it was still seeping fuel. so i decided to reinstall the oem fpr since it wasnt broken in the 1st place.

i also got new bolts to go into the iac motor, it used some 5 point torx or something like that. i took it out and examined it, spun it and it made sense why i was getting a drill like sound. it was catching a little on the inside, the bearing also did not feel smooth. installed a new o ring, greased it up some and reclocked the position of the iac, since there was a v cut in the ears of the bolt holes, whoever had it before wanted a lower idle? i started the car and warmed the car up idle is now at 850-900 warm. as im typing this im waiting for the ecu to reset, we'll see how this goes. either way just examining it has led me to believe it definitely needs to be replaced. if it doesnt work i believe the electric motor has failed and is not able to adjust the magnet to move the door open/close anymore.
post Sep 26, 2013 - 8:21 PM
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rdyzz

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so with the ecu reset, the car started out with a 3k rpm idle then went to 2k and stayed there for 10min. i drove it and it dropped down to 1,500 rpms but was surging when i would stop for the stop lights on 2 instances. after 20min it idles now at 1000 rpms. gonna have to order a new one now. this ones gone im sure of it.
post Oct 3, 2013 - 3:32 PM
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rdyzz

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found out the 2001 honda civic 1.7L iac is basically identical to the beams redtop. so i purchased one and am using it with excellent results.






post Oct 3, 2013 - 3:49 PM
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Smaay

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wow thats an awesome find!


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2001 Celica GT-S Turbo
1997 Supra TT 6speed
1997 Celica 3MZ/1MZ swap
1990 Celica All-Trac
post Oct 3, 2013 - 4:02 PM
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richee3



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That's some seriously cool stuff. thumbsup.gif If you don't mind me asking, how much did it cost? I still need to replace mine.


--------------------
"Employ your time in improving yourself by other men's writings, so that you shall gain easily what others labored hard for." -Socrates. Even Socrates told us to use the search button!

2006 Aston Martin V8 Vantage.
1998 Celica GT-
BEAMS Swapped.
2022 4Runner TRD Off Road Prenium.
2021 GMC Sierra AT4.

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