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> Alloy crank pulleys any good???
post Mar 20, 2014 - 2:05 PM
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Dudleydaftdog

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Hey all, thinking about binning my lightweight alloy crankshaft pulley for the stock iron harmonically balanced pulley as my new builds got a crank seal leak and I'm thinking this might have somethin to do with it???

Is anybody running an alloy one without any probs? Got it from Fensport so I thought it would be the business but can't decide whether to revert back to OEM tommorow while I have it off.

Any experience or thoughts on them would be muchly appreciated : )

Thanks

Chris
post Mar 21, 2014 - 10:19 PM
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Bezik777

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I'd say no due to lw pulley is not balanced...I've seen bad cases and seals gone out due to it..but 10 years ago I ran one on a GTI no problems after 30k...
post Mar 22, 2014 - 5:01 AM
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Dudleydaftdog

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Thanks Bezik777. That's good to know. Will give it another try after I've changed the seal and see what happens. Cheers. Chris.

PS struggling to get the crank pinion gear off now! Won't budge and can't get behind it to pull it... apart from a blow torch and a screw driver do you have and tips for removal? Thanks again.
post Mar 22, 2014 - 10:07 AM
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Smaay

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i highly recommend going back to stock crank pulley. i have seen too many cars with oil pumps explode because the balance was not there. you are not really gaining anything with the other pulley either.


--------------------
2001 Celica GT-S Turbo
1997 Supra TT 6speed
1997 Celica 3MZ/1MZ swap
1990 Celica All-Trac
post Mar 22, 2014 - 10:30 AM
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Dudleydaftdog

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Thanks Smay' gonna look for one asap. I'd rather lose 1 bhp than a little of oil a week. How does it affect the oil pump though its just powered by the cam belt? Thanks for your help :-)
post Mar 24, 2014 - 7:46 AM
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mkernz22



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I was looking into getting a lightweight pulley set, but after looking up reviews about lightweight ones, it isn't worth the issues it will cause.
It affects the oil pump because the stock pulley has a dampener on it to reduce the vibrations whereas the solid lightweight one doesn't.

It doesn't affect just the oil pump, but other areas of the engine as well.
Off an EVO forum:
"Originally Posted by GTREVO View Post
I have been an early user of underdrive pulleys for many years now but only learnt about the detrimental effects of harmonics in the 4G63 engine not too long ago.

Try replacing bearings every single race like I do and you will know that the problem lies more than just tolerances and balancing. Have been building 2.0 on the DSM's for years now and the inherent bearing problems but thank god I nitrided my cranks ( thus am able to save cranks even with worn out mains) and 2.3 strokers in my Evo 6 which kills absolutely every single mains running only 6 to 7 passes on a single event. And both makes over 700WHP. Both have not run harmonic balancers and without balance shafts. And yes, the engine DOES make a little more vibration without the balance shafts. Funny thing is that while the main bearings are worn out badly, the conrod bearings remain perfect, almost untouched....

Have recently completed a race on the stroker and will remove the main bearings shortly to compare previously on which I have ran no dampener and this time with the dampener. This will at least confirm some how on the effects of the dampener.

Am only relating my experiences with the harmonics that are killing the engine and I don't think Mitsubishi would be putting one on if it didn't need one...

If I recall in one of many early forums some long time ago, even Bushur runs the stock dampener and doesn't use pulleys...."

"Originally Posted by GTREVO View Post
Sorry for my late reply on my findings with my motor. Took it apart yesterday and the results are indeed very interesting. After running at over 8000 rpms on this stroker 2.3 motor and at 35 psi making 750 WHP/656 ft/ib WTQ, the bearings were in good reasonable condition and take note, this motor was run WITH a brand new stock Mitsubishi harmonic damper, crank pulley. I swear what I saw was surprising on what I revved the motor to ( 8500 rpm at times on the track). To add to the topic of balance shafts, this motor was built without balance shafts at all. The motor has seen done 40 dyno pulls and 10 full on passes down the track at the drags..

On my earlier post, I mentioned that the mains were worn right down to metal at a lower power level ( 670 WHP) and at less rpms at the track. This was on a brand new rebuilt motor with only 7 passes down the track and about 30 dyno pulls.

The above findings I found was on the same motor except that I replaced a set of brand new Clevites on it and the new Mitsubishi crank pulley and I was all ready to replace it again yesterday but hey there you go guys.... there is no dispute that the damper is there for a reason and for a very good reason in fact.... no more aluminium pulleys for me..."
post Mar 24, 2014 - 11:50 AM
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yellowchinaman



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there is also a good post in the GT4OC called "Why you should NEVER fit an Lightweight Alloy Crank Pulley"
Documented with lots of after effects including pictures of internal damage.

http://www.gt4oc.net/forums/viewtopic.php?...amp;hilit=pully
post Mar 24, 2014 - 11:58 AM
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Tigawoods



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QUOTE (yellowchinaman @ Mar 24, 2014 - 12:50 PM) *
there is also a good post in the GT4OC called "Why you should NEVER fit an Lightweight Alloy Crank Pulley"
Documented with lots of after effects including pictures of internal damage.

http://www.gt4oc.net/forums/viewtopic.php?...amp;hilit=pully

some of us arent blessed with access to gt4oc frown.gif


--------------------

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post Mar 25, 2014 - 8:08 AM
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Dudleydaftdog

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Guys can't thank you all enough for the info and help. Just bought a OEM one off fleabay. Running solid engine mounts with forged internals and tap happy hks cams and think the vibrations just too much for the crank without the harmonic balancer. Fingers crossed this should help with the crankseal oil leak. Given up tryin to get the crank gear off (just slid on when I built the engine?!?) So kinda half arsed it and tigersealed up the outside of the seal and reverted back to the stock balancer. Loving the 6g forum btw. You guys all RULE. Thanks again : )
post Mar 25, 2014 - 12:15 PM
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yellowchinaman



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Sorry Tigs.
Taken from the GT4OC:

QUOTE ("tbdevelopments")
I’ve been saying this for countless years to my customers not to fit the alloy crank pulleys in replacement of the standard Damper Pulley. Toyota did this for a reason and I’ve seen countless failures of the crank and quite a few with my own 2 eyes but up till now I have not recorded a failure, just did the repair as instructed. Well I had a customer come to me with a knocking coming from the bottom end of his GT4 ST205, the knocking sounded very much like a bigend rattle so I advised that if this was caught early enough we could drop the sump and as long as the crank was in perfect condition and the journal measurements came within specs and a plasti-guage final check we could get away with re-shelling the conrods, which basically means fitting new bearings with the crank in-situ and just bolt it all back up. If done correctly this is a perfectly adequate repair and will give many years of trouble free motoring. Conrod bearings will wear because of a few reasons, Age and power is the main one which is the conditions that give the most successful repair of this nature. The other is foreign material or metal entering the bearing or lack of oil, these will typically damage the crank which requires a bottom end partial rebuild.

Upon inspection of this car I noticed it had an alloy crank pulley fitted (pictured below)





The sump was dropped and the bearings were inspected, #1,2,4 were all in perfect condition. #3 was in a terrible state, extensive wear and a deep grove down to the base metal of the bearing. This was the cause of the knocking. The crank was inspected and seemed in good condition but found a small lump on the top of the journal which you could just feel with your finger tip, at the time it was facing the top of the engine so I was feeling blind. Believing at first to be a part of the bearing stuck to the surface I rotated the crank to give a better view but found this damage instead. There was a fine Hairline crack which ran almost 3/4 the way around the bearing journal of the crank, and in one part the surface had pushed upwards creating that small lump felt earlier, and the cause of the deep grove created in the bearing. Damage pictured below







The job was completed with a new set of bearing throughout, a replacement crank that was rebalanced, journals polished for clearance and rebuilt. The alloy pulley was also replaced with a factory item and the customer collected his car, Which had an initial fire-up and running-in by my to set the bearings and 300miles of normal driving before replacing the oil and going back to normal full boost operations.

The car this happened to only modification was an exhaust system; boost was even standard so power wouldn’t have exceeded 260bhp at the most. Yet the crank had failed. To put this into perspective we’ve done drag cars running over 900bhp with standard cranks without a single failure or even bend. Some models for testing were also extremely machined to remove any metal we could for revablity, they were machined like pieces of paper and at still exceeding 900bhp still not a failure. All these were fitted with the standard damper pulley. Yet this example failed at 260bhp with a pulley that could control the harmonics which had lead to its premature failure.

The reason behind the failure was Harmonic Resonance Failure. Without getting to in-depth I’ll keep the explanation simple but there are a few good examples for the technical minds amongst us on wikipedia.
http://en.wikipedia.org/wiki/Resonance
http://en.wikipedia.org/wiki/Harmonic_oscillator

Basically everything in the universe vibrates, whether it is the human body, sheet of metal, or in this case a crank. This is called its structural resonance frequency. Now this frequency is best expressed as a wave, with its peaks and troughs. And if you can generate an additional wave with the matching frequency (so the peaks and troughs match) the amplitude of that wave will grow, or the item will vibrate with more force, it’ll keeps growing until it structurally fails on a molecular level. To put this into everyday context you need to picture a swing with a fat man on it and your trying to push the swing with your little finger, Normally this isn’t going to happen but if you can get the swing started adding the small amount of force at the correct period, just at the peak of the swing you can over time make the swing oscillate higher and higher. This swing is the oscillation frequency and at the top of each swing is the peaks of the wave form and the base of the swing would be expressed as its trough. Now if you continued to keep adding this small force at the top of each swing the arc would eventually get higher and higher until either the swing broke or the fat man fell off, this would be the expression of the structural resonance failure. To stop this you need a simple damper that will effect outside frequencies (in our case the engine) or crank rotation from matching the frequency of the crank resonance. Going back to our fat man on the swing the damper would be effectively stopping the outside force, (you with your little finger) pushing on the swing at the correct time, for example before the swing meets its peak point, This would do nothing to aid the swing and certainly wouldn’t add force the its momentum making it arc higher and higher.

This is what the Toyota standard Harmonic Damper Pulley does, it removes harmonic resonance from the crank and additional frequencies causing the failures were seeing above.

For curiosity purposes I went all over the crank looking for more hairline cracks and found another around #2 journal leading into the counterweight but it was only very small, around 1cm in length but if left unattended would have grown like #3. So to see how far the resonance damage had gone I caused a controlled failure of the crank by putting in it a press until it snapped on the cracked areas. The pictures of this can be seen below. If you analyze the pictures you will see there are 2 different types of metal texture. The shinier, almost polished appearance is the damaged caused by the resonance; this is a failure on the molecular level and as you can see it quite extensive in #3 and starting to spread inwards on #2 just being visible on the outside edge. The other type is a more harsh texture, this was good metal until the press finished it off, this is typical of a pressure break where the cast material of the crank has basically shattered and all this was caused by me so ignore that. But it does show the 2 different types of damage, and how close this celiac came to complete destruction, where instead of a hairline crack and a rattley bearing the crank would have snapped pushing the rods out the side of the block casing and the entire engine unit would have been a total write-off.

Before people jump the gun and say “well I’ve got one and running 400bhp for years” this isn’t a situation where it’s a loaded gun at your head, where you fire you will die. It’s a situation where failures can/normally happen eventually, ranging from a matter of weeks to years, and from standard power up to 1000bhp. It’s a device which doesn’t address the base foundation of structural physics where the original Toyota unit does.

I hope this has enlightened people to the dangers of fitting an item like this, yes you will save around half the weight of the stock pulley but this really doesn’t add up to any noticeable gains in performance or revability and all its doing it radically effecting the longevity of the engine.











Tim smile.gif



QUOTE (yellowchinaman @ Mar 25, 2014 - 12:14 PM) *
Sorry Tigs.
Taken from the GT4OC:

QUOTE ("tbdevelopments")
I’ve been saying this for countless years to my customers not to fit the alloy crank pulleys in replacement of the standard Damper Pulley. Toyota did this for a reason and I’ve seen countless failures of the crank and quite a few with my own 2 eyes but up till now I have not recorded a failure, just did the repair as instructed. Well I had a customer come to me with a knocking coming from the bottom end of his GT4 ST205, the knocking sounded very much like a bigend rattle so I advised that if this was caught early enough we could drop the sump and as long as the crank was in perfect condition and the journal measurements came within specs and a plasti-guage final check we could get away with re-shelling the conrods, which basically means fitting new bearings with the crank in-situ and just bolt it all back up. If done correctly this is a perfectly adequate repair and will give many years of trouble free motoring. Conrod bearings will wear because of a few reasons, Age and power is the main one which is the conditions that give the most successful repair of this nature. The other is foreign material or metal entering the bearing or lack of oil, these will typically damage the crank which requires a bottom end partial rebuild.

Upon inspection of this car I noticed it had an alloy crank pulley fitted (pictured below)





The sump was dropped and the bearings were inspected, #1,2,4 were all in perfect condition. #3 was in a terrible state, extensive wear and a deep grove down to the base metal of the bearing. This was the cause of the knocking. The crank was inspected and seemed in good condition but found a small lump on the top of the journal which you could just feel with your finger tip, at the time it was facing the top of the engine so I was feeling blind. Believing at first to be a part of the bearing stuck to the surface I rotated the crank to give a better view but found this damage instead. There was a fine Hairline crack which ran almost 3/4 the way around the bearing journal of the crank, and in one part the surface had pushed upwards creating that small lump felt earlier, and the cause of the deep grove created in the bearing. Damage pictured below







The job was completed with a new set of bearing throughout, a replacement crank that was rebalanced, journals polished for clearance and rebuilt. The alloy pulley was also replaced with a factory item and the customer collected his car, Which had an initial fire-up and running-in by my to set the bearings and 300miles of normal driving before replacing the oil and going back to normal full boost operations.

The car this happened to only modification was an exhaust system; boost was even standard so power wouldn’t have exceeded 260bhp at the most. Yet the crank had failed. To put this into perspective we’ve done drag cars running over 900bhp with standard cranks without a single failure or even bend. Some models for testing were also extremely machined to remove any metal we could for revablity, they were machined like pieces of paper and at still exceeding 900bhp still not a failure. All these were fitted with the standard damper pulley. Yet this example failed at 260bhp with a pulley that could control the harmonics which had lead to its premature failure.

The reason behind the failure was Harmonic Resonance Failure. Without getting to in-depth I’ll keep the explanation simple but there are a few good examples for the technical minds amongst us on wikipedia.
http://en.wikipedia.org/wiki/Resonance
http://en.wikipedia.org/wiki/Harmonic_oscillator

Basically everything in the universe vibrates, whether it is the human body, sheet of metal, or in this case a crank. This is called its structural resonance frequency. Now this frequency is best expressed as a wave, with its peaks and troughs. And if you can generate an additional wave with the matching frequency (so the peaks and troughs match) the amplitude of that wave will grow, or the item will vibrate with more force, it’ll keeps growing until it structurally fails on a molecular level. To put this into everyday context you need to picture a swing with a fat man on it and your trying to push the swing with your little finger, Normally this isn’t going to happen but if you can get the swing started adding the small amount of force at the correct period, just at the peak of the swing you can over time make the swing oscillate higher and higher. This swing is the oscillation frequency and at the top of each swing is the peaks of the wave form and the base of the swing would be expressed as its trough. Now if you continued to keep adding this small force at the top of each swing the arc would eventually get higher and higher until either the swing broke or the fat man fell off, this would be the expression of the structural resonance failure. To stop this you need a simple damper that will effect outside frequencies (in our case the engine) or crank rotation from matching the frequency of the crank resonance. Going back to our fat man on the swing the damper would be effectively stopping the outside force, (you with your little finger) pushing on the swing at the correct time, for example before the swing meets its peak point, This would do nothing to aid the swing and certainly wouldn’t add force the its momentum making it arc higher and higher.

This is what the Toyota standard Harmonic Damper Pulley does, it removes harmonic resonance from the crank and additional frequencies causing the failures were seeing above.

For curiosity purposes I went all over the crank looking for more hairline cracks and found another around #2 journal leading into the counterweight but it was only very small, around 1cm in length but if left unattended would have grown like #3. So to see how far the resonance damage had gone I caused a controlled failure of the crank by putting in it a press until it snapped on the cracked areas. The pictures of this can be seen below. If you analyze the pictures you will see there are 2 different types of metal texture. The shinier, almost polished appearance is the damaged caused by the resonance; this is a failure on the molecular level and as you can see it quite extensive in #3 and starting to spread inwards on #2 just being visible on the outside edge. The other type is a more harsh texture, this was good metal until the press finished it off, this is typical of a pressure break where the cast material of the crank has basically shattered and all this was caused by me so ignore that. But it does show the 2 different types of damage, and how close this celiac came to complete destruction, where instead of a hairline crack and a rattley bearing the crank would have snapped pushing the rods out the side of the block casing and the entire engine unit would have been a total write-off.

Before people jump the gun and say “well I’ve got one and running 400bhp for years” this isn’t a situation where it’s a loaded gun at your head, where you fire you will die. It’s a situation where failures can/normally happen eventually, ranging from a matter of weeks to years, and from standard power up to 1000bhp. It’s a device which doesn’t address the base foundation of structural physics where the original Toyota unit does.

I hope this has enlightened people to the dangers of fitting an item like this, yes you will save around half the weight of the stock pulley but this really doesn’t add up to any noticeable gains in performance or revability and all its doing it radically effecting the longevity of the engine.











Tim smile.gif



Still want shiny alloy light weight pulleys?
post Mar 25, 2014 - 1:20 PM
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Syaoran



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Lightweight pullies are retarded on any inline 4 cylinder engine. On top of that, they're even more stupid to put on our engines because of this:

Before balancing my engine (a stock, unmolested engine): http://i269.photobucket.com/albums/jj61/ar...zps21870d82.jpg
After balancing: http://i269.photobucket.com/albums/jj61/ar...zpsd6bb870d.jpg


The balance on the engines from Toyota is, at best, "what's necessary" for the engine to last a lifetime driven below 4000 RPMs.


--------------------
1993 Celica GT Coupe - sold
1994 Celica GT Liftback
post Mar 25, 2014 - 2:25 PM
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mkernz22



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I'm pretty glad I didn't spend the money on a pulley set yet.
I'm still going to get one, hopefully, but just ask for everything except the crank pulley. That would include PS pump, Alt, and the A/C delete one.
I should be fine as long as I'm using the oem crank pulley, right?
post Mar 25, 2014 - 7:39 PM
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Syaoran



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The crank pulley is the only important one I would say, because it's not just a pulley. It's rubbed filled which is intended to absorb harmonic vibrations i.e. a harmonic balancer.


--------------------
1993 Celica GT Coupe - sold
1994 Celica GT Liftback
post Mar 29, 2014 - 11:49 AM
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Dudleydaftdog

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Feel a bit sick... My forged fresh built engines knocked since about 500 miles into the break in. Put it down to the solid engine mounts Think i know why all of a sudden! I used ACL race series bearings throughout, would this help save the bottom end or would you guys think its game over? When i say knock, it s a gentle one at tickover, oils been changed every 100 miles or so and i also slick 50'd it after break in. Its never been above 4k since i built her (still mapping her). I'm also running high lift cams so its been harder to notice as they are more "tap happy". Gonna fit the OEM pulley this week n hopefully it should improve... Think I need a beer : $
post Mar 31, 2014 - 9:41 AM
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mkernz22



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QUOTE (Dudleydaftdog @ Mar 29, 2014 - 12:49 PM) *
Feel a bit sick... My forged fresh built engines knocked since about 500 miles into the break in. Put it down to the solid engine mounts Think i know why all of a sudden! I used ACL race series bearings throughout, would this help save the bottom end or would you guys think its game over? When i say knock, it s a gentle one at tickover, oils been changed every 100 miles or so and i also slick 50'd it after break in. Its never been above 4k since i built her (still mapping her). I'm also running high lift cams so its been harder to notice as they are more "tap happy". Gonna fit the OEM pulley this week n hopefully it should improve... Think I need a beer : $


If the knock is already there, then swapping out to the OEM crank won't change anything. It'll only prevent anymore damage.

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