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> Why am I boosting at 12?, Still stock, thought max at stock was 10...
post Dec 4, 2005 - 11:11 PM
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Green_MachToy

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I had a stud in the Exhaust manifold break at the head. In repairing it, my car is now pushing 12 pounds. I still have the stock ecu, no boost controller (until tomorrow), no FCD (stock max is 9.7). Now to give you a few more specifics: A friend of mine put a plastic t in my lines to trick the wastegate into allowing more boost. This caused me to reach 10 (probably 9.7, but meter isn't that detailed). In doing the repair I took the t out. I also found that my Cat was bad and took it out as well (it will cost me $300 to fix later). Replaced a crush gaskit after the stock down pipe to the 3" exhaust. Got everything together at approx 0130, and took it for a test drive. Found a couple of vacuum lines had worked themselves off of the stock BOV. Fixed those, and off again. Ran at stock 7 pounds of boost. Placed the t back in, ran at 10. Next day...got in the car got on it to pass a car...14! Took the t out, down to 12! It does seem to creep. When I hit the gas, it will jump to about 8-10, then steadily walk up to 12 as the rpm's increase. Did my wastegate go bad? I was thinking the increased flow in the exhaust from having no cat may have been the problem but it ran stock the night I did everything. Any ideas?

This post has been edited by Green_MachToy: Dec 5, 2005 - 8:34 AM
 
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post Dec 4, 2005 - 11:38 PM
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lagos



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what motor are you talking about? it looks like you have a 3rd gen 3sgte. thats stock boost for that motor.

who did your swap?

This post has been edited by lagos: Dec 4, 2005 - 11:39 PM


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post Dec 5, 2005 - 1:23 AM
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Green_MachToy

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QUOTE(lagos @ Dec 5, 2005 - 4:38 AM) [snapback]363317[/snapback]

what motor are you talking about? it looks like you have a 3rd gen 3sgte. thats stock boost for that motor.

who did your swap?

Sorry...missed that important piece of info. Yes, it is a 3sgte 3rd gen. A couple of friends and I did it in my garage. I thought the max stock boost for the 3rd gen was 9.7?! Even if that was the case I was running at 7 and 10 max when I completed the repairs. Then the next morning I was running at 14 and 12. I don't understand why when nothing changed between that night and the morning.

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