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Enthusiast ![]() Joined Mar 21, '04 From Oceanside Currently Offline Reputation: 2 (100%) ![]() |
I had a stud in the Exhaust manifold break at the head. In repairing it, my car is now pushing 12 pounds. I still have the stock ecu, no boost controller (until tomorrow), no FCD (stock max is 9.7). Now to give you a few more specifics: A friend of mine put a plastic t in my lines to trick the wastegate into allowing more boost. This caused me to reach 10 (probably 9.7, but meter isn't that detailed). In doing the repair I took the t out. I also found that my Cat was bad and took it out as well (it will cost me $300 to fix later). Replaced a crush gaskit after the stock down pipe to the 3" exhaust. Got everything together at approx 0130, and took it for a test drive. Found a couple of vacuum lines had worked themselves off of the stock BOV. Fixed those, and off again. Ran at stock 7 pounds of boost. Placed the t back in, ran at 10. Next day...got in the car got on it to pass a car...14! Took the t out, down to 12! It does seem to creep. When I hit the gas, it will jump to about 8-10, then steadily walk up to 12 as the rpm's increase. Did my wastegate go bad? I was thinking the increased flow in the exhaust from having no cat may have been the problem but it ran stock the night I did everything. Any ideas?
This post has been edited by Green_MachToy: Dec 5, 2005 - 8:34 AM |
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![]() Enthusiast ![]() ![]() ![]() ![]() ![]() Joined Aug 31, '02 From Philadelphia, PA Currently Offline Reputation: 8 (100%) ![]() |
what motor are you talking about? it looks like you have a 3rd gen 3sgte. thats stock boost for that motor.
who did your swap? This post has been edited by lagos: Dec 4, 2005 - 11:39 PM -------------------- 15PSI - 30MPG - Megasquirt Tuned
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Enthusiast ![]() Joined Mar 21, '04 From Oceanside Currently Offline Reputation: 2 (100%) ![]() |
QUOTE(lagos @ Dec 5, 2005 - 4:38 AM) [snapback]363317[/snapback] what motor are you talking about? it looks like you have a 3rd gen 3sgte. thats stock boost for that motor. who did your swap? Sorry...missed that important piece of info. Yes, it is a 3sgte 3rd gen. A couple of friends and I did it in my garage. I thought the max stock boost for the 3rd gen was 9.7?! Even if that was the case I was running at 7 and 10 max when I completed the repairs. Then the next morning I was running at 14 and 12. I don't understand why when nothing changed between that night and the morning. |
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