!!5sfte!!, the second coming! |
!!5sfte!!, the second coming! |
Nov 17, 2007 - 3:13 PM |
|
Enthusiast Joined May 12, '06 From Wilmington, NC Currently Offline Reputation: 45 (100%) |
yep, you heard me. I'm coming back to the 5sfte community. Doing things a little different this time around, here's what I can remember so far that I'm doing differently:
Genuine HKS BOV, the new 2007 design Got my injectors cleaned and flow tested at witchhunter. They were is poor condition before and are great now! Going with a SAFCII instead of a neo. I got it for about $75 cheaper, and it measures knock. I was gonna get a greddy emanage ultimate, but I don't have a laptop to tune it with and it just looked too complicated for me to figure out how to tune it by myself, so maybe I'll upgrade later. Got a custom stailness braided oil feed and drain line kit made specifically for my 5sfte. I just gotta weld a fitting onto my oil pan but I'm having a hard time finding someone willing to do it. I'm fixing my radiator fan which was broken before. the motor fell out of the blade cause it was hooked up wrong I'm using a regular sized radiator instead of the koyo, for a little more engine bay room I'm relocating the battery to the trunk and I'm cutting my IC piping down a lot for a cleaner install, might even paint them like LewFX that's all I can think of right now, pictures to come. hope to be running by the end of the week after 6 months of down time! -------------------- 94 GT - Sold -------- 69 Pontiac Lemans - Sold 88 Alltrac - Sold ---- 04 WRX - Sold 00 GT-S - Sold ------ 91 Miata - project/drift car 95 GT - Sold -------- 96 GT - New Daily Drive |
Dec 8, 2007 - 2:03 AM |
|
Enthusiast Joined May 12, '06 From Wilmington, NC Currently Offline Reputation: 45 (100%) |
well, I put it back together today. I got fed-up with having to wrench away at those two bolts that hold the fuel line in place so I went out and bought a wratcheting wrench. No I didn't have any before, and now I know what I've been missing! It normally took me like 15-20 minutes to get those two bolts in or out cause a ratchet can't fit in there, this time it took less than 2 anyway, I got everything fixed that I wanted to. in fact, I even was able to fix my alarm which had been broken since before I had even turbo-ed because I couldn't figure out why it was broken. I know I had shorted two wires accidentally, but I had checked all fuses and nothing was blown. well, while I had the engine in shambles I discovered a well-hidden wire that definately does not seem stock and it had a fuse outside the main fuse boxes, well, replaced that fuse and it works now. lol
The only thing I'm severly pissed about is that my wideband gauge is no longer working! the gauge gets power, but the signal is all F'ed up. it would read some wierd things like saying I was super lean at idle even though I could smell the gas and I knew I was super rich. then it worked for a bit and told me I was at a 13.7 AFR after I had leaned out idle about to get the car to smooth out, so that seemed right. but then at times is would just sit at some strange number like 14.1 and just stay there at idle, low, and full throttle. I checked all the connections for the signal and it should be working right. I'm wondering if the tip of the sensor is too fouled to get a good reading (it was very black from me running so rich), or if the sensor itself was somehow damaged in the time it spent out of my car... I dunno, but this gauge was expensive and I'm very sad it's not working. anyway, no more gas leaks, no more coolant leaks, but some oil leaks have reared their ugly heads. The first time around, for the filter relocation kit, I had put teflon tape on all the threads and it never leaked from any threads, then I was told that teflon tape should only be used on the AN threads and not the NPT threads, so I put teflon only on the AN threads this time around and now it's not leaking from any AN threads, but it's leaking from ALL the NPT threads on the relocation kit and the oil drain line... it's not soo bad though. As long as I top it off with oil every day it should be ok to drive short distances. I might try to get teflon tape on all those NPT threads tomorrow after work, but we'll see. only other thing is, I need to find some uber small hose clamps or somthing, cause my car likes to blow vacuum lines off the intake manifold! I noticed while I was driving it that my BOV stopped working and I could hear compressor surge, and then my car wouldn't idle lower than 2000 rpms. I blew the vacuum hose for the BOV off, and for the idle control valve. lol. -------------------- 94 GT - Sold -------- 69 Pontiac Lemans - Sold 88 Alltrac - Sold ---- 04 WRX - Sold 00 GT-S - Sold ------ 91 Miata - project/drift car 95 GT - Sold -------- 96 GT - New Daily Drive |
Dec 8, 2007 - 7:12 AM |
|
Moderator Joined Oct 1, '02 From fall river, ma Currently Offline Reputation: 13 (100%) |
QUOTE(6strngs @ Dec 8, 2007 - 3:03 AM) [snapback]620842[/snapback] well, I put it back together today. I got fed-up with having to wrench away at those two bolts that hold the fuel line in place so I went out and bought a wratcheting wrench. No I didn't have any before, and now I know what I've been missing! It normally took me like 15-20 minutes to get those two bolts in or out cause a ratchet can't fit in there, this time it took less than 2 anyway, I got everything fixed that I wanted to. in fact, I even was able to fix my alarm which had been broken since before I had even turbo-ed because I couldn't figure out why it was broken. I know I had shorted two wires accidentally, but I had checked all fuses and nothing was blown. well, while I had the engine in shambles I discovered a well-hidden wire that definately does not seem stock and it had a fuse outside the main fuse boxes, well, replaced that fuse and it works now. lol The only thing I'm severly pissed about is that my wideband gauge is no longer working! the gauge gets power, but the signal is all F'ed up. it would read some wierd things like saying I was super lean at idle even though I could smell the gas and I knew I was super rich. then it worked for a bit and told me I was at a 13.7 AFR after I had leaned out idle about to get the car to smooth out, so that seemed right. but then at times is would just sit at some strange number like 14.1 and just stay there at idle, low, and full throttle. I checked all the connections for the signal and it should be working right. I'm wondering if the tip of the sensor is too fouled to get a good reading (it was very black from me running so rich), or if the sensor itself was somehow damaged in the time it spent out of my car... I dunno, but this gauge was expensive and I'm very sad it's not working. anyway, no more gas leaks, no more coolant leaks, but some oil leaks have reared their ugly heads. The first time around, for the filter relocation kit, I had put teflon tape on all the threads and it never leaked from any threads, then I was told that teflon tape should only be used on the AN threads and not the NPT threads, so I put teflon only on the AN threads this time around and now it's not leaking from any AN threads, but it's leaking from ALL the NPT threads on the relocation kit and the oil drain line... it's not soo bad though. As long as I top it off with oil every day it should be ok to drive short distances. I might try to get teflon tape on all those NPT threads tomorrow after work, but we'll see. only other thing is, I need to find some uber small hose clamps or somthing, cause my car likes to blow vacuum lines off the intake manifold! I noticed while I was driving it that my BOV stopped working and I could hear compressor surge, and then my car wouldn't idle lower than 2000 rpms. I blew the vacuum hose for the BOV off, and for the idle control valve. lol. nate, you have the teflon tape thing backwards. you never have to use tape on AN fittings, they are a pressure fit. NPT on the other hand, requires the thread tape. -------------------- Former Team 5SFTE pro member ;)
13.6@108MPH, 5SFTE Powered |
Lo-Fi Version | Time is now: November 28th, 2024 - 2:34 PM |