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> Beams Throttle Body to Rev 3
post Jan 29, 2015 - 12:01 AM
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Kiolofunk

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What's up 6GC?! I'm Kiolo and I'm from the Philippines.

I recently swapped over a 3sge rev 3 motor into my AE101 with celica brakes, not that anyone's interested. wink.gif

As the title suggests, I'm looking into swapping over a 3sge beams throttle body into my 3sge rev 3. Reason is my iacv went bad and i found a beams tb from a local yard with an iacv on it. Unfortunately, they won't sell the iacv alone so i went in and made the purchase.

I've tried bolting it up and it seems right on, however, i was wondering what would be the effects of the larger inlet/outlet? I'm thinking that there really wouldn't be any power difference, possibly but not that much. Mileage consumption perhaps a little bit higher? Not really sure. Can someone enlighten me?

Thanks in advance!

post Jan 29, 2015 - 9:51 AM
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Smaay

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if it bolts up and the TPS signal is good, then the larger TB will give you a slight increase of power. acceleration might be a little more responsive. thats about it.


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2001 Celica GT-S Turbo
1997 Supra TT 6speed
1997 Celica 3MZ/1MZ swap
1990 Celica All-Trac
post Jan 29, 2015 - 10:30 AM
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njccmd2002



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And it will look cool


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post Nov 2, 2015 - 5:50 PM
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Kiolofunk

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Bringing the thread back to life. I have only gotten to bolt this over the weekend and all seem fine except for two things:

1. One bolt doesn't line up. (I was thinking of doing a spacer adaptor) but comes problem 2 below
2. TPS plugs are different. Mine has 4 wires and the BEAMS unit has 3. rolleyes.gif

Problem has really worsen as my idle drops to 500 when idle and sometimes it's erratic (500-800rpm) but if i unplug the IACV sensor then it revs back to normal. Also, it makes a hissing sound when the idle drops and goes up. This hissing sound also isn't present when the IACV sensor is unplug.

Cleaning the valve doesn't seem to make much of a difference now. It seems that the valve doesn't really fully close/open which causes the problem.

I'll head over to the scrapyard next week and find another TB. Hope it's for the Rev 3 this time. If anyone needs the BEAMS TB with TPS and IACV let me know.

Has anyone else experienced this issue?
post Nov 3, 2015 - 8:04 AM
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Bitter

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Can you move the IACV valve back and forth smoothly? It should move easily, if it's stiff or doesn't move then it's bad. It's a common problem for these to go bad either where they don't move smoothly or the electrical parts get weak and can't move the flap fast enough.


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post Nov 4, 2015 - 9:00 PM
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Kiolofunk

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Thanks for your response. Yeah it moves freely although I'm not quite certain why it doesn't fully close, like it leaves a gap. Not sure if that's how it's supposed to be. I tried one of my buddy's IAC sensor (from 4AGE) they look really identical so i gave it a shot and it is still the same. So I am leaning towards more on the mechanical valve itself. I'll post a vid up when i get a chance.
post Nov 4, 2015 - 9:18 PM
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doory100



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sounds like your TB cable is to long and its not opening the TB enough. I had the same issue with my 1mzfe TB on my 5s custom intake. so I made a bracket. should have painted it..



This post has been edited by doory100: Nov 4, 2015 - 9:19 PM


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post Nov 8, 2015 - 2:10 AM
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Kiolofunk

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Good point though my cable is short. I actually wanted a longer one due to the cable hanging in the middle of the intake and it's being pressed by my strut bar (the plastic hose was cut open) so i had to remove my strut bar in the mean time. I don't think this is my problem though. Haven't gotten the time to post up a vid as I rarely use the car. Need you guys to see it to understand the problem I guess.

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